Here is an addendum to my earlier post in 2020 about changing fluid. I added clarification and some different ways to do it.
This is an addendum to my 2020 fluid changing notes. This is what I did when converting from the
older “yellow” Century fluid to the newer Rohmer fluid. I still went with my theory to minimize fluid
waste and not create air pockets. I did
NOT flush my system with distilled water or DI water. I preferred not to introduce any potential of
adding anything that might be corrosive (including water). Thus our system only had old fluid, maybe a
small air bubble here or there and the new fluid.
Expansion tank
To clarify, the fluid line GOING TO the expansion tank is on
the lower right side. The molded
reservoir has a lower depression in that area.
(This is counter intuitive to me, I would think that the suction would
be from the lowest possible point. This
would permit some operation, just in case one was low on fluid.) There may be other reasons that I am not
aware. Here’s a picture. Inlet to the reservoir is to the right. Suction from the reservoir is center, elightly left.
Note I have a plumbing “test plug” as my cap, as our original
cap didn’t fit very well. We did get
some splashing out of that reservoir into our closet. The test plug has worked well enough that I
haven’t been motivated to change the reservoir yet.
Removing excess fluid
My previous procedure to remove the excess fluid was to put
a tube down the inlet and suck the fluid out with a small pump (drill pump, or
similar).
This time, I removed the drain plug from the Alde System and
only let out a slight amount of fluid. I
just drained the reservoir dry, plus maybe a little more. (It was maybe a quart of fluid, that’s it.) That prevented the introduction of air
bubbles. I reinserted the plug, but didn’t
reinstall the hose clamp, YET!
The drain of our 2018-CS trailer is located about 10 inches
ahead of the drivers-side tire.
I then did the earlier procedure to flush out the old and
replace with new fluid. That system has
worked well for me. If you have both
rubber adapters inserted into the fittings on the bottom of the reservoir,
there is no leakage. (You don’t have to
press very hard ether.)
After that was completed, I drained out the tiny amount of
old fluid that was in the drain area. I just
removed and quickly reinserted the drain plug.
It was a little messy, but was done quickly. Maybe there was ½ cup of fluid. THEN you can reinstall the hose clamp on the
drain.
Other trailer model thoughts:
I have used my setup on our 2018-CS (no bathroom) and an
earlier 320. We had sufficient room to
use that setup. Alde used to have a
setup that they would lend (with a deposit) to users but that was prior to them
being part of Truma. Note that their
setup is a little shorter overall. The
suction side only draws from the reservoir tank, which would not capture the
older fluid very well. Here is a picture
from an older Alde manual.
Oh yeah, I put a footswitch on the pump. That allowed me to hold the plumbing adapter in place and start things rolling. I had one assistant that checked the color of the fluid and supplied the new fluid when needed.
I tried the shop vac method and it worked great at getting all the fluid out. <...>
I have a 2015 Max-S and, now retired, finally got around to doing this myself -- in preparation to address anticipated convector corrosion. I decided to go this route to eliminate the need to push more than two gallons of new glycol in (while pushing out the old). I can report that it worked well for me, and that I won't hesitate to do it again.
I am now intimately familiar with the workings of my Alde system. (I will report on the corrosion adventure in another thread.)
My approach is something like this:
Ensure Alde system is off at control panel
Remove energy for Alde heat (unplug from 120VAC power and close propane)
Open the drain valve at bottom of trailer and collect old glycol from the internal reservoir
Disconnect hose at top of Alde unit (under the bench) to break vacuum and drain additional glycol
Reconnect hose at top of Alde and disconnect hose at bottom of Alde (so that shop-vac suction does not drive the circulation pump)
Remove cover from Alde reservoir
Use shop vac (with attachments) to suck glycol from the reservoir (where the return hose at the center bottom enters the reservoir) to remove remainder of system glycol
Reconnect the hose at bottom of Alde
Close the bottom drain valve
Refilling with either distilled/deionized water to flush, or with new glycol, the approach is the same:
Set circulator pump speed to 5 (under the bench, red arrow nominally set at 3)
Using a large funnel or a hand pump, fill internal reservoir (to the max line)
Turn on Alde system at control panel, and set thermostat so that it asks for heat
When the circulator pump empties the reservoir, turn off the Alde system and refill the reservoir
Repeat this process (3, 4) until the fluid level stabilizes
Run the system for several minutes to remove air (automatic)
Top off the fluid in the reservoir so that it is near the max line
Reset the circulator speed to 3, button things up and restore heat sources (120VAC, propane)
Using this approach, I collected, then added, just short of 2 gallons. A water flush retained some color, but I think this method removes essentially all of the fluid for practical purposes.
Thanks for everyone who described their approaches and experiences here. It was (and continues to be) extremely helpful to me.
Enquiring minds will need to know: what sizes are those nicely done PVC pipes? And, those "rubber "gaskets"? How did you make those, or are they some sort of standard part? Fittings/adapters for the PVC to the shop vac pipe?
Here is some information about the "suction adapter" --
I did not glue these pieces together, nor did I tape them.
The two black neoprene washers are 2" OD and 1/2" ID (measured), with one cut down to 1.5" OD. I got them at Ace Hardware. Prior to insertion in the glycol reservoir, I put the washers at the lower end of the short pipe, with the smaller diameter one at the bottom. They slide up a little, and differently, as the pipe descends and everything gets seated.
Hope that helps someone!
2015 T@B S-Max towed by 2016 Subaru Outback 3.6R -- central Pennsylvania "Travel is fatal to prejudice, bigotry and narrow-mindedness." Mark Twain, The Innocents Abroad, 1869
Enquiring minds will need to know: what sizes are those nicely done PVC pipes? And, those "rubber "gaskets"? How did you make those, or are they some sort of standard part? Fittings/adapters for the PVC to the shop vac pipe?
This is really going to help some owners who may have issues getting easy access to the expansion tank.
I used the shop vac procedure when changing Alde fluid and found it completely drained the system. I had bulging issues so had to remove the convectors to make repairs. There was no fluid in the system after draining. 2016 T@B QMax.
2016 T@B 320 Qmax, 2020 KIA Sorento, The Woodlands, TX
Enquiring minds will need to know: what sizes are those nicely done PVC pipes? And, those "rubber "gaskets"? How did you make those, or are they some sort of standard part? Fittings/adapters for the PVC to the shop vac pipe?
Thanks, I edited my original post/comment.
2015 T@B S-Max towed by 2016 Subaru Outback 3.6R -- central Pennsylvania "Travel is fatal to prejudice, bigotry and narrow-mindedness." Mark Twain, The Innocents Abroad, 1869
@glesieutre Thank you very much. It is always nice to see the mods to the mods. @Dalehelman , who developed the "shop vac" idea, would approve, I'm sure.
- I'm assuming you used an external fluid pump between the fresh Alde source and the input hose connection (not the Alde pump), which pump did you use? - Did you notice any level change in the reservoir during this transfer? - Do you have any info on the hoses you used to connect to the bottom ports to the fill/return jugs?
Thanks.
2022 T@B 400 Boondock 2015 RAM 1500 Outdoorsman Quad Cab South Jersey
When I do this again I will use two of these pumps. One to push the replacement glycol in with and one to help pull out the old. I found the gravity draining needs a bit of help and I didn't like the idea of using a powered vacuum. The reservoir does drop when pushing the fluid in but with an additional pump it will go faster.
The hoses that come with the pump are good enough to complete the project, I just used a couple of barbed fittings and a 1/2" MPT/FPT to couple together from the local ACE hardware store to adapt from one hose size to another. I will edit later when I can take a picture. I also poured the 3.5 gallons of glycol into a new clean bucket so I didn't have to keep moving the hose out of one bottle of fluid to another. Since the hose curls up at the bottom of the bucket I weighed it down with another filled bottle to keep the hose at the bottom.
I am preparing to do the DIY glycol fluid exchange on my 2018 320S using the adapters fabricated out of 3/8" OD copper toilet supply tube with the #2 drilled out stoppers, the Performance Tool hand pump, etc. The instructions and the schematic indicate that the inlet adapter through which the new fluid is pumped is to be modified (with two 45 degree bends) and goes into the offset opening and not the opening directly below the expansion tank opening on top. In looking at my tank, it wasn't clear to me that that is correct. Feeling the tubes coming out of the bottom of the expansion tank (since I can't see them) it seems that the rubber tube that is attached to the direct opening goes to the circulator pump and Alde boiler which would make it the intake and that the rubber tube coming out of the offset opening bends toward the direction of the convectors which would make it the outlet. How am I going wrong on this? I'm sure the answer to this is somewhere in the forum but I haven't found it.
2018 T@B 320S. Tow vehicle: 2020 Toyota Hylander Hybrid
@jalars8, you may not be wrong. The flow schematic shown in the DIY manual is consistent with what is shown in Alde's literature, and with the way my 2015 is configured.
That said, I vaguely recall at least one other report of the expansion tank in a newer T@B being plumbed in the opposite manner. I don't know if this is an official change to the installation protocol, or just something done out of convenience when the campers are assembled. Regardless, you are well served to confirm the orientation of the hookups on your own unit.
From a functional perspective, I doubt it makes much of a difference how those lines are hooked up.
When I used the shop vac method I placed the vac suction on the hole directly below the fill opening. This completely pulled all the fluid out of the system on our 2016 T@B QMax.
2016 T@B 320 Qmax, 2020 KIA Sorento, The Woodlands, TX
@jalars8 I'm not sure if there has been changes as @ScottG said was possible, but the picture attached shows how our 2020 320S is plumbed. The pump draws glycol from the tanks offset port. From there the glycol is pushed through the Alde and heated. It then passes through the convectors before returning to the center port in the expansion tank. I believe that it draws from the higher port in the expansion tank so that there is less chance of debris being sucked into the pump.
Stockton, New Jersey 2020 nuCamp T@B 320S * Jeep Wrangler
My tank is different but can't provide a photo because of its position. On my tank, the offset opening is on the left (left of the direct opening) and is also the lower opening. It looks like with my tank, it draws from the higher port in the direct position and the fluid comes back through the lower port to the left.
2018 T@B 320S. Tow vehicle: 2020 Toyota Hylander Hybrid
I wonder if the design of the tank has changed with regard to which port is offset. Regardless, the three preceding reports all indicate that the outflow (i.e., back to the Alde via the circulator pump) is through the higher port, and the return (from the convectors) is through the lower port.
It's never been explicitly clear why the posts are at different levels, but this is the configuration shown in the Alde manuals.
I bought a 2019 Tab 320S about a month ago. The Alde appeared to be running fine for a test run of a couple hours. The previous owner had never changed the fluid so I knew I would need to check for corrosion after reading numerous post and watching videos, mainly from Mark on you tube and after finding this forum, Scott G. with his very informative instruction manual for Alde fluid change. I have installed some new hose pieces , after shortening the corroded convection ends, ( about an inch or so from each end on both back convectors). I have some fluid and preparing for the refill. I have a few questions hopefully can be answered here. 1. Has anyone that shortened their convectors noticed any changes in performance? 2. Has anyone put a shut-off valve at the drain plug location to facilitate a more controlled drain flow? 3. Has anyone put any isolating valves at strategic locations to facilitate removal of specific components? 4 Has anyone needed to replace their auto-bleed assembly and / or non-return valve, and if so , why ?
Many thanks to all that have shared their experiences here!
@Paul1 great stuff! Do you have any photos of the corrosion you found? Was it as "bulgy" as the images you saw in Mark Turney's video? The video shows some "worst case" scenarios. There have been a whole range of corrosion noted in the threads, all the way down to completely collapsed convector "stubs".
If you haven't seen it: there is a whole thread about the corrosion here, and several owners have cut off corroded stub ends, or even taken out parts of the "convectors" to gain new "stub ends" to connect hoses.
That is another huge thread, but if you page through and look at photos, etc, you should find the owners who had to modify their convectors because of corrosion. Most owners just needed to clean the corrosion away.
2: Why hasn't anyone thought of this before? There are several threads where owners had the entire glycol drain under the trailer swept away by road debris. A valve makes a lot of sense.
3. If you have read through this thread, there have been many modifications to various things like changing the tank location, and adding various valves at the correct spots to make removing the glycol easier. There are several places in the trailer where it would seem easy to "block" the flow from one segment to the other. Or places that can be opened and make the draining of the glycol even easier. (The 180 degree bend on my 2017 at the end of the convector under the passenger bench comes to my mind.) The longer you stare at the Alde, and look over this thread, the more some of these things seem obvious.
I opened up my glycol loop at the "non return" valve to drain my glycol. This is one of the "points of attack" the smart owners here discovered while back engineering the glycol loop. I took out the valve to clean it and had a look at it. It is an aluminum tube, with a plastic valve inside that appears pretty robust. There have been failures of this valve due to corrosion, etc. The biggest problem seems to be techs who don't remember how the valve should be installed, put it in backwards, and....glycol won't flow. An owner over at Facebook had their glycol changed, and the techs put the valve in backwards. Apparently, they were too lazy to go through the whole "run the pump to drive out the air process". When the owners discovered there was no heat, they were advised to "turn the pump up to 5" to drive the air out of the system. And, eventually burned out the pump!
I suppose the non-return valve can fail without being corroded, etc, but I'm not sure if anyone has reported that happening.
Many times in the various glycol changing threads owners have shown there is more than one way to get this job done, and deal with the Alde in general. There have been several modifications to the basic process. When different owners with different skills put their own creative ideas into this, the whole process will improve and change.
@pthomas745 Thank you for your reply. I refilled my system with what I believe is the same product that was in before, the Century yellow/green. I had also replaced the check valve I ordered from Truma. The old one was allowing flow in either direction. I had also filled the main unit with glycol while I was taking my time to work on the other parts. Before the refill, I actually drained out the main unit and double checked the glycol for any debris or tell tale signs of the condition of it. All looks good for now. I then just took the hand pump that Scott G. had recommended and put the discharge hose into the alde tank through the input line back to the pump. It only took a couple of minutes the see the glycol flowing back to the tank. System seems to be running fine so far with no alarms . I did get a few pictures of the convector ends. There was similar to most I have seen here. I actually pulled off the hoses and checked every connection as well. I did replace the 5 aluminum connectors with the new plastic ones. Hopefully I do not see the bulges again for a while . I am thank for this forum and everyone that contributed their experience , that enabled me to move forward to complete this project. I am not sure yet which way I will go for the next time. Perhaps the extra drain on the passenger side could be the easiest. I will likely be tempted to pull off a couple of clamps anyway just to check the convector ends.
@Paul1 on your list of questions... #1: I had to shorten my long convectors in the rear because I couldn't find new replacements at the time I needed them. I had to remove about 2.5" of the "fins" which I calculated to be about 3.5% of the total finned area so I know it's less efficient but very minimally and it wasn't noticeable at all.
I did add a second drain "T" on the opposite side of my T@b at the same general location as the original drain (both are at the low points of the system). This did make draining the most amount of liquid from my system much more effective. To @pthomas745 point though I did double my chances of road rubble draining my glycol by ripping off my drain! After thinking about that a bit I think I might install something on the undercarriage to act as a bit of a block to fend off the offending rubble and maybe save my drain tube and glycol.
Comments
This is an addendum to my 2020 fluid changing notes. This is what I did when converting from the older “yellow” Century fluid to the newer Rohmer fluid. I still went with my theory to minimize fluid waste and not create air pockets. I did NOT flush my system with distilled water or DI water. I preferred not to introduce any potential of adding anything that might be corrosive (including water). Thus our system only had old fluid, maybe a small air bubble here or there and the new fluid.
Expansion tank
To clarify, the fluid line GOING TO the expansion tank is on the lower right side. The molded reservoir has a lower depression in that area. (This is counter intuitive to me, I would think that the suction would be from the lowest possible point. This would permit some operation, just in case one was low on fluid.) There may be other reasons that I am not aware. Here’s a picture. Inlet to the reservoir is to the right. Suction from the reservoir is center, elightly left.
Note I have a plumbing “test plug” as my cap, as our original cap didn’t fit very well. We did get some splashing out of that reservoir into our closet. The test plug has worked well enough that I haven’t been motivated to change the reservoir yet.
Removing excess fluid
My previous procedure to remove the excess fluid was to put a tube down the inlet and suck the fluid out with a small pump (drill pump, or similar).
This time, I removed the drain plug from the Alde System and only let out a slight amount of fluid. I just drained the reservoir dry, plus maybe a little more. (It was maybe a quart of fluid, that’s it.) That prevented the introduction of air bubbles. I reinserted the plug, but didn’t reinstall the hose clamp, YET!
The drain of our 2018-CS trailer is located about 10 inches ahead of the drivers-side tire.
I then did the earlier procedure to flush out the old and replace with new fluid. That system has worked well for me. If you have both rubber adapters inserted into the fittings on the bottom of the reservoir, there is no leakage. (You don’t have to press very hard ether.)
After that was completed, I drained out the tiny amount of old fluid that was in the drain area. I just removed and quickly reinserted the drain plug. It was a little messy, but was done quickly. Maybe there was ½ cup of fluid. THEN you can reinstall the hose clamp on the drain.
Other trailer model thoughts:
I have used my setup on our 2018-CS (no bathroom) and an earlier 320. We had sufficient room to use that setup. Alde used to have a setup that they would lend (with a deposit) to users but that was prior to them being part of Truma. Note that their setup is a little shorter overall. The suction side only draws from the reservoir tank, which would not capture the older fluid very well. Here is a picture from an older Alde manual.
TV: 2017 Toyota Highlander
TV: 2017 Toyota Highlander
I am now intimately familiar with the workings of my Alde system. (I will report on the corrosion adventure in another thread.)
My approach is something like this:
- Ensure Alde system is off at control panel
- Remove energy for Alde heat (unplug from 120VAC power and close propane)
- Open the drain valve at bottom of trailer and collect old glycol from the internal reservoir
- Disconnect hose at top of Alde unit (under the bench) to break vacuum and drain additional glycol
- Reconnect hose at top of Alde and disconnect hose at bottom of Alde (so that shop-vac suction does not drive the circulation pump)
- Remove cover from Alde reservoir
- Use shop vac (with attachments) to suck glycol from the reservoir (where the return hose at the center bottom enters the reservoir) to remove remainder of system glycol
- Reconnect the hose at bottom of Alde
- Close the bottom drain valve
Refilling with either distilled/deionized water to flush, or with new glycol, the approach is the same:- Set circulator pump speed to 5 (under the bench, red arrow nominally set at 3)
- Using a large funnel or a hand pump, fill internal reservoir (to the max line)
- Turn on Alde system at control panel, and set thermostat so that it asks for heat
- When the circulator pump empties the reservoir, turn off the Alde system and refill the reservoir
- Repeat this process (3, 4) until the fluid level stabilizes
- Run the system for several minutes to remove air (automatic)
- Top off the fluid in the reservoir so that it is near the max line
- Reset the circulator speed to 3, button things up and restore heat sources (120VAC, propane)
Using this approach, I collected, then added, just short of 2 gallons. A water flush retained some color, but I think this method removes essentially all of the fluid for practical purposes.Thanks for everyone who described their approaches and experiences here. It was (and continues to be) extremely helpful to me.
{edit}
Here is some information about the "suction adapter" --
The black connection to the shop vac rigid tube is a: "2-1/2 in. Power Tool Adapter Accessory Shop Vac Attachment." I got it at Home Depot: https://www.homedepot.com/p/RIDGID-2-1-2-in-Power-Tool-Adapter-Accessory-Shop-Vac-Attachment-for-RIDGID-Wet-Dry-Vacuums-VT1407/100206293. Perhaps it could be adapted for other diameters, or something similar is available for other brands. The smallest diameter is called 1", but the ID is just less than 7/8". I might have used duct tape on the shop vac side.
The long pipe is a 3/4 in. x 2 ft. CPVC Water Supply Pipe. The actual OD is 7/8". https://www.homedepot.com/p/Charlotte-Pipe-3-4-in-x-2-ft-CPVC-Water-Supply-Pipe-CTS-12007-0200R/203019298. It's a tight fit into the preceding adapter, but the adapter is flexible, and it works.
The short pipe is a 1/2 in. x 2 ft. CPVC Water Supply Pipe, cut to 11.25 in. length. The actual OD is 5/8". https://www.homedepot.com/p/Charlotte-Pipe-1-2-in-x-2-ft-CPVC-Water-Supply-Pipe-CTS-12005-0200R/203019249 Others might have to adjust this length to ensure clearance above the back shelf, to minimize height, or to ensure it is downhill to the shop vac.
The connecting elbow is a 3/4 in. x 1/2 in. CPVC-CTS 90-Degree Slip x Slip Reducing Elbow Fitting. https://www.homedepot.com/p/NIBCO-3-4-in-x-1-2-in-CPVC-CTS-90-Degree-Slip-x-Slip-Reducing-Elbow-Fitting-U4707R3412/100346346
I did not glue these pieces together, nor did I tape them.
The two black neoprene washers are 2" OD and 1/2" ID (measured), with one cut down to 1.5" OD. I got them at Ace Hardware. Prior to insertion in the glycol reservoir, I put the washers at the lower end of the short pipe, with the smaller diameter one at the bottom. They slide up a little, and differently, as the pipe descends and everything gets seated.
Hope that helps someone!
"Travel is fatal to prejudice, bigotry and narrow-mindedness." Mark Twain, The Innocents Abroad, 1869
Thanks, I edited my original post/comment.
"Travel is fatal to prejudice, bigotry and narrow-mindedness." Mark Twain, The Innocents Abroad, 1869
Nice.
- I'm assuming you used an external fluid pump between the fresh Alde source and the input hose connection (not the Alde pump), which pump did you use?
- Did you notice any level change in the reservoir during this transfer?
- Do you have any info on the hoses you used to connect to the bottom ports to the fill/return jugs?
Thanks.
2015 RAM 1500 Outdoorsman Quad Cab
South Jersey
2020 nuCamp T@B 320S * Jeep Wrangler
1. Has anyone that shortened their convectors noticed any changes in performance?
2. Has anyone put a shut-off valve at the drain plug location to facilitate a more controlled drain flow?
3. Has anyone put any isolating valves at strategic locations to facilitate removal of specific components?
4 Has anyone needed to replace their auto-bleed assembly and / or non-return valve, and if so , why ?
Many thanks to all that have shared their experiences here!
#1: I had to shorten my long convectors in the rear because I couldn't find new replacements at the time I needed them. I had to remove about 2.5" of the "fins" which I calculated to be about 3.5% of the total finned area so I know it's less efficient but very minimally and it wasn't noticeable at all.
I did add a second drain "T" on the opposite side of my T@b at the same general location as the original drain (both are at the low points of the system). This did make draining the most amount of liquid from my system much more effective. To @pthomas745 point though I did double my chances of road rubble draining my glycol by ripping off my drain! After thinking about that a bit I think I might install something on the undercarriage to act as a bit of a block to fend off the offending rubble and maybe save my drain tube and glycol.
Posting here for an update on method and results.
https://tab-rv.vanillacommunity.com/discussion/17441/anybody-done-a-diy-glycol-exchange-on-a-400#latest
2019 T@B400 Boondock Lite "Todd"